I repaired a broken shift lever bracket on a GSXR motorcycle today. The upper cast aluminum bracket broke off cleanly when the owner laid the motorcycle down.
Attachment 1371
I prepped it for welding by grinding the fractured surface and old threads (and a little paint around the edges) down to fresh metal with a carbide burr. I also added a sheet metal heat shield to protect the grease-laden chain and plastic chain guard behind the area to be welded.
Attachment 1372
Then I built up fresh, solid aluminum using TIG (using as much as 200 amps, with no pulse, and about 65-70% EN AC balance), using up a good length of a 1/8" 5356 filler rod. The trick I find on a "long distance" build-up operation like this is to take your time and do it in as many layers is is necessary, allowing the work to cool in between layers to maintain control of the shape. If you don't try and get too big of a blob molten all at once, you can control the final built-up shape with some precision. I also had my digital calipers set up and locked at the desired distance I needed the material to be built up to, which allowed me to quickly check progress of the build-up operation and know when I had added enough material.
Attachment 1373
Then I got out a new aluminum-specific 4.5" grinding wheel and using my angle grinder, tried that out to surface the front face of the built-up material down flat (and in the plane the bracket needed it to be. The aluminum-specific grinding wheel worked very quickly and effectively! It left a smoother surface than I would have guessed and also worked very quickly without loading up. (Like a flap disc does on aluminum.) Here is what the aluminum grinding wheel looks like:
Then it was just a matter of lining up the bracket, scribing where the hole needed to be drilled, drilling and tapping the hole squarely. I tried using pam as a tapping fluid and I found it worked really well, didn't need to re-apply it once. Best tapping fluid I've found for aluminum so far.
I would have cleaned up around the outer edges of the built-up area with a rod-shaped carbide burr I've got that would have made it look as if it were CNC machined, but the customer didn't seem to care much about cosmetics in this area of the bike (and wanted to save a few bucks), so I skipped it as he instructed me to.
Attachment 1376
The lower bracket was bent in a little bit from the crash, so I used a crescent wrench and baby sledge hammer to persuade it back out just a little bit. It didn't take much. Overall the repair worked out quite successfully in the end! Customer was happy.
Attachment 1375
Here is the shot of the bike after being repaired. It looked pretty fast. The customer had it tricked out with some fancy aftermarket stuff too.
Attachment 1374