Howdy Folks! I'll assume that most of you aren't aware that my daily transportation is a v10 powered 2001 f250 4x4 crew cab. Great truck, obscene torque, and an overall joy to drive...until you pull up to the gas pump. Average 11-12 mpg. I've seen 14.5, and I've seen 6.7 pulling a 10,000 lb trailer, whigh it pulled @77mph no problem. Well, It's aggravating my already precarious financial situation to continue with this as my main mode of transport. So, a couple of mnths ago, I was driving past this old caravan that never seemed to move. One day as I was driving by, the owner of said van was in the driveway, so I stopped to ask about it. He said that it had a cracked block, and he just wanted it OUT of his driveway. A deal was struck, and I ended up as the new owner, and as it turns out, the van still started and drove, but not well enough to preclude me towing it the 75 miles up to my place, and the hunt for a replacement engine. Through a series of connections, and a very good friend using up one of his last "I owe you one" chips,I ended up with a used caravan engine, SAME model year, 122,000 alleged miles, sitting on a stand at my place. Well, it goes without saying that whenever one has this particular engine (3.0 Mitsubishi v6) ready to install, It is highly advised to replace the head gaskets, head bolts, and timing belt.
Once I got the engine stripped down and the heads removed, I was disappointed to see that the front left piston rings had left a "rust ring" around the bore, indicating that moisture had gotten into the cylinder and it had sat. Here's a "before" pic
After careful consideration of numerous factors, including the fact that it looks worse than it feels, I decided that I would check a few things, and if all looked right, I would attempt to hone out the "bad" spot in the bore, and allow the existing rings to re-seat, once back together. First, I checked the ring end gap. Factory spec is .012-.018" with a service wear limit of .031" These checked out @ .016" Leaving me MILES of life if this works out. The guy I bought the motor from offered me the option of a different motor, but that means $70.00 in gas, and a day shot driving to get it done, plus re-doing all the work I've done thusfar, so I decided this would be the best and quickest option. I started out with the rigid hone below, using a LOW SPEED drill, and spraying wd40 to keep the stones cutting,
After a few minutes, I had managed to get 99% of the damage out of the bore, but the worry of taper, bellmouthing, and over-cutting had me stop. I checked my work, and decided to finish up with a dingleberry hone. like this
Notice how the end is missing the dingleberries, and that shaft is sticking WAT out there? This is going to possibly hit the crankshaft so, One cutoff tool and 30 seconds gave me this
I used it to get the final angled crosshatch pattern, and the bore ended up looking like this
I cleaned the bore out, and measured the bore, and the ring end gap. All said and told, I ended up removing less than .001" from the bore, with no taper or bellmouthing to speak of, and the "ring" is all but gone.
I inspected the rod bearings, and pulled another rod cap for good measure, and thay look excellent.
The rings appear to be chrome faced, so now, my only concern is whether they will seat correctly on the fresh surface that I just created. The top ring on the "problem" piston was actually stuck in the groove a bit. So, I had to coax it out of the groove and clean things up and allow the ring to move freely enough to give itself it's proper tension. My hope is that it seats itself up in a relatively short time and goes into normal operation. I'd guess a quick oil change after an hour of running, followed by another 1,000 miles later, and It'll be as if nothing was ever amiss. More to come on this project....lots more