I've had glass bead in my blast cabinet for probably 6 months or longer, sometimes too much, sometimes not aggressive enough, but enough of a PITA to change that I dealt with it. Had a pump head repair the other day, needed walnut (badly scaled aluminum and brass parts), so I did the swap. 45 minutes of scooping, blowing, vacuuming, etc. Well, started on some other projects and neither media was aggressive enough, needed aluminum oxide or something else. Found Coal Slag from TSC for $8 a bag. Figure it'll crush down, I can screen it and have a finer grit and just dump it each time it dies.
Not wanting to keep spending 45+ minutes to swap, I decided to modify the bottom of the cabinet. Cheapie from Harbor Freight
Bought it a few years back from a friend for next to nothing.
The bottom of the media area tapers on 4 sides to a rectangular area (ALL pics taken with cabinet laying on it's back on a work table)
That little pipe does diddly squat to empty it, even with a vacuum hose on it. Pulled the pipe stub
Not much to work with. Tossed around several ideas, a cap, a trapdoor, etc. Came up with a sliding door. First thing is to cut the bottom, just above the curve, then weld a patch over the existing hole (or what's left of it) I thought about a round piece and pretty fit up, all tigged and shiny, then said 'screw it, I'll never see it and a surface patch is more than enough. I did cut the bottom of the hole out so it was U shaped and therefore wouldn't trap ANY media
Cut two 'runners' from 3/4x3/32(?)" angle iron. Beveled the front corners to make the door easier to get back on.
NASTY mill scale and surface. 40 grit discs and several minutes got it that cleaned up (more cleaning later). Took one or three shots, finally got the MIG dialed in nice for some downhill 18ga to 1/8" edge joints. Welded the top of the angle iron leg as well as the bottom corner (all scale cleaned up in the weld areas really well) Got some pieces cut and cleaned, 14ga (I think) sheet, some 3/32(?)" x3/4" flat and some 1x1/8" zinc coated crap I don't even know why I had.
Burned them together nicely, the welds look cold, but there was plenty of penetration. Didn't feel the need to run the whole edge, so a few 3/4" long welds down the side, then I ground the area that would mate to the sheet steel.
Lined one up with the edge of the sheet, clamped it in place on the runner and started tacking. I welded just about the whole length, skipping as I went. I don't have a shot of it, but after the first, I put a piece of 1/16" TIG rod in the channel on the left side, then clamped the right side in nice and tight. Once I had both sides, I put a piece across the bottom (back) to make sure it wouldn't go too far and welded a piece of angle for a handle
Before someone points out the gap on the front and back edges, the intent was to leave it a loose fit so not to grind the hell out of everything each time. A piece of foam (or folded paper towel) keeps the grit from running out those gaps and is easier to replace than a chewed up slide.
You'll notice all the millscale is gone now, I knew it would be a snug fit, so I welded it up, knocked the slide out and then ground the bottoms of the runners till it was gone, which gave me just the right clearance to operate it smoothly.
I hadn't bothered cleaning out the last bits of walnut shell before I started, so I figured it was as good a test as any. Put it back in place and used an air nozzle to blow all the remaining media to the bottom, thumped the sides a few times to get everything loose, then pulled the handle.
Why the hell didn't I do this two years ago, I expect media changes will take about 5 minutes now, 10 if I do a really thorough job and wipe down the inside (I only do that when changing to FINER grit. I could care less if there's some walnut in my coal slag...)
Took a bit longer than I thought, but I learned one very very important lesson. When you have a hood with grind mode, ALWAYS CHECK IT BEFORE YOU STRIKE AN ARC!